To properly torque down the carrier bearings, I made this special tool out of a piece of flat steel with two bolts and a wheel nut.
To achieve proper carrier bearing preload, they recommended I use approx 80 - 100lb-ft of torque on them! A power bar was required to do that job eventually..
Next was setting the backlash between the gears. Gear backlash is the free play normally felt between gears. This free play is there to allow for proper lubrication of the gears. Proper lubrication prevents wear on the gears and helps keep them cool when running hard. The manufacturer recommended 0.008" of backlash, measured using a dial gauge with a magnetic base.
At this point, we now begin to check to see if the pinion depth (set via the shims mentioned earlier) was chosen correctly. There is no correct spec for this, you need to start with an average spec, assemble the 3rd member, then check if the gears are meshing properly. Depending on the mesh pattern (see below pics), you will have to either add or minus shims to get the correct depth.. and everytime you get it wrong, you need to disassemble EVERYTHING just to change those shims..
A section of the gears was painted and the ring gear was turned back and forth a few times (to intersect with the pinion gear) to get an idea on how they mesh. (See the problem with buying used stuff, this 3rd had went through hell by the previous owner, somehow his pinion tried to eat the differential housing!!
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This is the drive side of the gears. Notice how the markings are centered on the tooth.. a Perfect mesh pattern!
This is the coast side, similar story with the mesh pattern.. ideal..
Of course it took me a few tries to get them to that point, initially the drive side was marked way off to the inside of the ring. (The coast side was to the outside of the ring). By adding more shims, I was able to bring both of them to the center.. Once the required mesh pattern is achieved, a crush collar can then be installed for the pinion bearings. You ONLY crush that collar until you get the required bearing preload, then stop right there. I used Loctite to lock the pinion nut in place.
I have been driving on these gears for approx 2 weeks now and they run dead silent! and the power regained is superb! I previously ran 30" MTs on my Vit (up from the stock 27"s) and the power loss was significant. Now I am running 31"s and it feels like the stock 27"s, even with my dead engine..
Special thanks goes out to Imtiaz for the technical assistance during this build. Thanks also goes out to Khameel for the use of his tools + the technical assistance. Finally would like to thank my brother (Runul) and Brian for the parts they played during my build..
Hope others will benefit from this..